2008-21-01: We are adopting a new airworthiness directive (AD) for certain Hawker Beechcraft Corporation Model BAe.125 series 800A (including C- 29A and U-125) airplanes, and Hawker Beechcraft Model Hawker 800XP airplanes. This AD requires doing an inspection to determine the serial number and part number on the main landing gear (MLG) upper casing, and replacing the MLG assembly with a serviceable MLG assembly if necessary. This AD results from a report indicating that the MLG casings have received improper hydrogen embrittlement relief. We are issuing this AD to prevent a fracture of the MLG casings and a collapse of the affected MLG, which could adversely affect the airplane's continued safe flight and landing.
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2008-16-05: The FAA is superseding an existing airworthiness directive (AD) for RRD Dart 528, 529, 532, 535, 542, and 552 Series turboprop engines. That AD currently requires a dimensional inspection of the intermediate pressure turbine (IPT) disk or an ultrasonic inspection of the seal arm contact between the high pressure turbine (HPT) and the IPT disk seal arm and reworking or replacing the IPT disk if worn beyond acceptable limits. This AD continues to require those actions. This AD results from us including an incorrect engine model and omitting an engine model from the applicability of the existing AD. We are issuing this AD to prevent HPT disk failure, which can result in an uncontained engine failure and damage to the airplane.
DATES: This AD becomes effective September 4, 2008. The Director of the Federal Register previously approved the incorporation by reference of certain publications listed in the regulations on February 26, 2007 (72 FR 2610, January 22, 2007).
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2008-19-03: We are adopting a new airworthiness directive (AD) for certain Boeing Model 737-300, -400, and -500 series airplanes. This AD requires repetitive external detailed inspections or non-destructive inspections to detect cracks in the fuselage skin along the chem-mill steps at stringers S-1 and S-2R, between station (STA) 400 and STA 460, and repair if necessary. This AD results from reports of cracks in the fuselage skin common to stringer S-1 and between STA 400 and STA 460. We are issuing this AD to detect and correct fatigue cracking of the fuselage skin panels at the chem-mill steps, which could result in sudden fracture and failure of the fuselage skin panels, and consequent rapid decompression of the airplane.
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2008-19-07: We are adopting a new airworthiness directive (AD) for the products listed above. This AD results from mandatory continuing airworthiness information (MCAI) originated by an aviation authority of another country to identify and correct an unsafe condition on an aviation product. The MCAI describes the unsafe condition as:
All DHC-8 Series 400 aircraft have had a spoiler fuselage cable disconnect sensing system installed in production. Subsequently it was discovered that, in the event of a spoiler fuselage cable disconnect, only the ROLL SPLR INBD HYD caution light will be illuminated until the aircraft speed decreases below 165 kts [knots], at which time the ROLL SPLR OUTBD HYD caution light will also be illuminated. In the event of a spoiler fuselage cable disconnect in association with the existing indications described above, the reduction in roll authority could result in increased pilot workload during approach and landing.
* * * * *
We are issuing this AD to require actions to correct the unsafe condition on these products.
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2008-20-02: We are adopting a new airworthiness directive (AD) for the products listed above. This AD results from mandatory continuing airworthiness information (MCAI) originated by an aviation authority of another country to identify and correct an unsafe condition on an aviation product. The MCAI describes the unsafe condition as:
A few hydraulic system tube clamps located inside the wing fuel tanks were found damaged. Further analysis has shown that damage to multiple clamps may cause sparks inside the tanks, which in turn may lead to ignition of flammable vapors inside the fuel tanks.
We are issuing this AD to require actions to correct the unsafe condition on these products.
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2008-19-09: We are adopting a new airworthiness directive (AD) for the products listed above. This AD results from mandatory continuing airworthiness information (MCAI) originated by an aviation authority of another country to identify and correct an unsafe condition on an aviation product. The MCAI describes the unsafe condition as:
Service experience has shown that heavy MLG (main landing gear) shimmy vibration can occur due to faulty/empty dampers or due to excessive free play in the T/L (torque link) apex joint. In several cases this shimmy vibration resulted in a MLG main fitting failure *
* * finally resulting in a collapse of the MLG causing extensive
damage to the wingtip, aileron and flaps. * * *
We are issuing this AD to require actions to correct the unsafe condition on these products.
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2008-19-12: The FAA is adopting a new airworthiness directive (AD) for Honeywell International Inc. TFE731-4, -4R, -5, -5AR, -5BR, and -5R series turbofan engines, with interstage turbine transition (ITT) duct, part number (P/N) 3075292-1; 3075292-3; 3074766-1; 3077063-1; 3075655- 1; 3075655-2; 3075699-1; or 3075699-3, installed. This AD requires replacing the affected ITT duct with a serviceable and redesigned ITT duct. This AD results from reports of 49 low-pressure turbine (LPT) blade separation events. Six of those events resulted in circumferential failure of the LPT2 or LPT3 nozzle assembly, leading to deformation of the ITT duct and uncontainment of the turbine blades and fragments of the LPT nozzle assembly. We are issuing this AD to prevent uncontainment of turbine blades and fragments of the LPT nozzle assembly, which could result in damage to the airplane.
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2008-16-13: We are adopting a new airworthiness directive (AD) for certain Boeing Model 737-600, -700, -700C, -800, -900, and -900ER series airplanes. This AD requires replacing the pushrods for the left and right elevator tab control mechanisms with new, improved pushrods. This AD results from a report of a rod end fracture on a rudder power control unit (PCU) control rod, which is similar to the ones used for the elevator tab pushrods. Analysis revealed that the fractured rod end had an incorrect hardness, which had probably occurred during the manufacture of the control rod. We are issuing this AD to prevent fracture of the elevator tab pushrod ends, which could result in excessive in-flight vibrations of the elevator tab, possible loss of the elevator tab, and consequent loss of controllability of the airplane.
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2008-19-02: We are superseding an existing airworthiness directive (AD) for Bell Helicopter Textron Canada (Bell) Model 222, 222B, 222U, 230, and 430 helicopters. That AD currently requires visually inspecting the main rotor hydraulic actuator support (support) to verify the presence of all dowel pins and sealant between the support and transmission and verifying the proper torque of each attaching nut (nut). This AD requires the same actions as the existing AD and also requires repetitive actions at intervals not to exceed 600 hours time-in-service (TIS) or 12 months, whichever occurs first. This AD is prompted by the discovery that a 12-month compliance requirement was correctly included in an Emergency AD (EAD) that we issued but was inadvertently omitted when we published the Final rule; request for comments following the issuance of the EAD. The actions specified by this AD are intended to prevent failure of the support and subsequent loss of control of the helicopter.
DATES: Effective October 16, 2008.
The incorporation by reference of Bell Helicopter Textron Alert Service Bulletin Nos. 222-00-86, 222U-00-57, 230-00-18, and 430-00-17, all dated May 19, 2000, was approved previously for incorporation by reference by the Director of the Federal Register on March 2, 2001 (66 FR 10361, February 15, 2001).
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2008-18-10: We are adopting a new airworthiness directive (AD) for certain McDonnell Douglas Model MD-90-30 airplanes. This AD requires a detailed inspection for certain defects of the upper fasteners of the aft mount support fitting of the left and right engines and corrective actions if necessary. This AD results from reports of loose, cracked, or missing fasteners in the aft mount support fitting of the left and right engines. We are issuing this AD to detect and correct loose, cracked, or missing fasteners in the engine aft support mount fitting, which could lead to separation of the support fitting from the pylon, which could result in separation of the engine from the airplane.
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